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Old 24th August 2019, 18:53
Beeyar Wunby's Avatar
Beeyar Wunby Beeyar Wunby is offline  
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Furthermore, Rail is saying that "human error is thought to be the main cause of a Caledonian Sleeper train running away through Edinburgh Waverly"

No surprises there then. But they do add something interesting...
Quote:
Originally Posted by Rail Magazine
1) Initial indications from sources suggest that when shunting at Carstairs, the red brake isolation cock had been turned off (sic, ) behind the 92, meaning that only the locomotive brake was available.

2) A source told Rail that during the design stage of the coaches, concern had been raised that the component 'went the wrong way' and could be moved by staff accidently
So that might account for how the brake pipe was closed off from the loco. However this should have been noticed if the brake tests required by the rule book (listed earlier in this thread) had been carried out.

They also mentioned..
Quote:
Originally Posted by Rail
Questions have also been raised regarding the running brake test, with a source questioning if the 92 did not give an accurate reading. However both CS and GBRf dismissed this.
Which is right because a personal (static) brake test only requires the driver to observe the brake gauges moving up and down, it doesn't prove the brakes are working. What really tells you what's going on is a running brake test, which looks for 'retardation' (a drop in speed). You both feel this in the seat of your pants & see it on the speedo. And if a running brake test wasn't conducted, someone is definitely in the doghouse.

We continue to watch with interest.

BW
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